Starting doing logs again for the Flex Fuel tune. Started off with pure corn....ran through the 10 mile drive, then the 4th gear 1,500-4K WOT hit, and then 4th gear WOT full pull. Everything looks great.
Car has about a 1/4 tank of corn in her and then I fill the tank to about half with 93, do some more logs. Everything looks great.
Run that tank to almost gone, fill up half way with 93, and run that almost out to make sure there really are no more remnants of corn in the system. Fill up full tank of fresh 93 and start the logging again. Get to the 4th gear WOT hit and during the pull my fuel pressure sensor shits the bed around 6K rpm
Injector duty on the run shot through the roof and I was getting a bunch of knock retard.
I can't order up just the fuel pressure sensor for the car, so I have to buy a whole new set of fuel rails with the sensor
That shit comes in and I swap it out really quick. I start logging from the 10 mile drive again to make sure the car isn't fooked. Car is running well, get the final pull done and send the logs in. Get a message back that I am getting knock from 6,200-redline. Tuner is worried something is wrong with the motor
I pull all 16 plugs on this fat bitch to make sure everything looks ok. This job is a major PITA on these cars, took me like 3-4 hours. Plugs look good, so then I am thinking maybe I picked up some bad fuel from Shell. I run out my current tank and refill with some BP 93. I do another pull and I am still seeing KR! I am getting super frustrated, Curt tells me to get the car up in the air and look over the exhaust because he is very confident in his knock sensor settings. He has seen cars pick up knock for exhaust making contact under the car. Sure as shit the catback was making contact on the driver's side trunk area.
So I pull the exhaust off of the car which was a lot of fun, thank god for a map gas torch and beer. I get the car back together with proper clearances everywhere and go datalog some pulls to see if I am picking up any KR. That did the trick, the KR was gone! What a fucking sense of relief, I thought there was a strong possibility my motor was hurt.
I wrapped up some 1st through 3rd WOT pulls on 93 and everything looked good, no KR.
So where I sit today is I need to do some 1st through 3rd WOT pulls on corn and then I will be done. The car is an animal, a bit of a handful with the manual, but I love it. It absolutely shreds the tires and pulls hard. I don't have final dyno numbers yet, but it should put down around 810 rwhp. Super happy with the car even though it felt like she was fighting me the whole way. Very thankful that I was using such an awesome tuner.