Have the mph...106.7 high and average about 105mph
Got a few bugs and can't seem to pull the number
Have made the suspension better, need to re-tighten everything down, weld up the torque boxes up and need an alignment!
Upgraded to a 11'' clutch and have the adjustable clutch cable/quad setup, but it is a single quad and I need the double hook piece to dial the system in. In other words, it is not at optimum engage/release settings.
At the SCT Dyno tune I found out I was running real lean. Jerry thought I had a bad MAF, but I found what I think is the problem was the next day. I have the complete WMS cold air kit and the rubber throttle body connecting part lost the clamp that holds the inlet tube. I am sure it was pulling un-metered air in after the MAF. Guessing extra unaccounted air would cause a lean situation???