ive gotten a couple pm's about how the car did, well i thought i'd post it up lol. ended up not even making a complete pass before i chipped a couple pistons......i can't blame anyone but myself, but i DID have the car tuned at zzp, and it WAS exactly how i pulled it off the dyno....I really don't know what happened, as my laptop must have died on the launch, from being throw into the back seat area (i knew i shoulda got a mount!). The wb02 was at 11.7-11.8 the whole time, and i was running 108 unleaded fuel. should have been okay, but the added timing musta been too much. I had an issue with 5*kr right after i got home, and matt said it was because the car was heatsoaked. I believed him....well...maybe he was right, but it wasnt heatsoaked this time....
couple pics of the carnage....
couple pics of the carnage....