First pass - All Motor. 3.0" pulley, C16, ~19* timing. The car went 12.9 at 104mph with a 1.8 60ft. Best ET it's ever done on the motor, and probably the worst trap speed. You can definitely tell the motor is getting worse for making power. It's all hole shot.
Mo-Kan 1/4 mile dragway GTP runs 12.9 - YouTube
Next was spraying a 125 shot. The car cut a 1.7 60ft and went 12.3 at around 110mph. Got a large amount of knock, as I think there may have still been some 87 octane in the line.
Mo-Kan 1/4 mile dragway GTP runs 12.3 - YouTube
Next run, I pulled timing back. Also on a 125 shot, it cut a 1.7 60ft and went 11.8 at 114mph. The car felt great on this pass. Trap speed is still 2mph less than it was in Tulsa a year ago.
Mo-Kan 1/4 Mile Dragway GTP runs 11.8 - YouTube
Last run, I went for a 175 shot. Spun hard out of the hole, gripped, and then snapped what I'm assuming is the input shaft. I may have had too much air pressure in the tires, so it could have been my own fault.
Mo-Kan Dragway GTP breaks input shaft - YouTube
Anyways, the car went 11.8 3 times over the past year, along with a WHOLE bunch of low 12 second passes. Plus a few nights of street racing during the summer. I can't really ask much more out a stock internal, 168K mile 4T65E. Although, if my 2nd stage would have actually worked like it was supposed to, I may have gotten pretty close to that 10 second timeslip.
Mo-Kan 1/4 mile dragway GTP runs 12.9 - YouTube
Next was spraying a 125 shot. The car cut a 1.7 60ft and went 12.3 at around 110mph. Got a large amount of knock, as I think there may have still been some 87 octane in the line.
Mo-Kan 1/4 mile dragway GTP runs 12.3 - YouTube
Next run, I pulled timing back. Also on a 125 shot, it cut a 1.7 60ft and went 11.8 at 114mph. The car felt great on this pass. Trap speed is still 2mph less than it was in Tulsa a year ago.
Mo-Kan 1/4 Mile Dragway GTP runs 11.8 - YouTube
Last run, I went for a 175 shot. Spun hard out of the hole, gripped, and then snapped what I'm assuming is the input shaft. I may have had too much air pressure in the tires, so it could have been my own fault.
Mo-Kan Dragway GTP breaks input shaft - YouTube
Anyways, the car went 11.8 3 times over the past year, along with a WHOLE bunch of low 12 second passes. Plus a few nights of street racing during the summer. I can't really ask much more out a stock internal, 168K mile 4T65E. Although, if my 2nd stage would have actually worked like it was supposed to, I may have gotten pretty close to that 10 second timeslip.